I have a Thermal Arc 211 Inverter TIG/Stick welder that I bought to leave and develop my skill in TIG welding. It worked fine at first. The torch was a large 26 size and for what I was looking to do, I moved to a smaller 17 size.
I immediately noted that my electrode would become red hot, the arc was diffused and wandering, lots of contamination in the weld, etc. I blamed me as I was just learning but after lots of reading, I decided gas was not getting to the torch head. I had flow from the regulator to the inverter but not the torch. No obstructions in the torch lines.
I took it to the approved warranty center. they discovered the gas line inside the welder was too long. When I attached the new 17 torch and tighten the fitting, the gas line behind the fitting twisted onto it's self and completely blocked the gas flow. They cut the line down and reattached fittings. Torch works perfectly now and I don't feel like a total idiot. Still need a lot of seat time but my skill is improving because the equipment is working properly now.
I immediately noted that my electrode would become red hot, the arc was diffused and wandering, lots of contamination in the weld, etc. I blamed me as I was just learning but after lots of reading, I decided gas was not getting to the torch head. I had flow from the regulator to the inverter but not the torch. No obstructions in the torch lines.
I took it to the approved warranty center. they discovered the gas line inside the welder was too long. When I attached the new 17 torch and tighten the fitting, the gas line behind the fitting twisted onto it's self and completely blocked the gas flow. They cut the line down and reattached fittings. Torch works perfectly now and I don't feel like a total idiot. Still need a lot of seat time but my skill is improving because the equipment is working properly now.