Hi all, been a little while since an update, but I think the machine is mechanically 100% done. There are still a few code changes and features I want to work on, but it all seems to be working great. I ran my first part since the update last night and it FLEW. Super excited. Here is the progression to where I am today:
Cables were carefully routed up the side of the machine and the back of the column. I decided to use the bottom of the machine cabinet as storage for the extra cable length of the spindle and Y axis motor cables. The yellow cables are M12 cordsets that connect to the PDB push button, solenoids, and the PC (power). The blue cables are Ethernet to the Smoothstepper and RS485 to the drives.
I used a Greenlee punch set to knock two holes in the cabinet. Grommet edging was wrapped around the sharp edge and all the cables were pulled. The front hole was a last minute decison to allow easier storage/access to the cables for the 4th axis motor.
Cable route across the monitor stand and loop into the bottom of the industrial PC. I had hoped to get them closer to the same length, but you can't see it behind the screen.
I noticed the spindle was making a little noise and discovered the spindle tophat was rubbing on the pull plate. There was only a .005" gap on each side, so it isn't surprising.
I chucked the piece (fully assembled) in my lathe and indicated the off center hole into alignment, then took a skim cut to open it up a few more thou. This really fixed all the noise coming from the spindle.
I continued on my quest to get the spindle perfect by measuring the installed depth of the tophat relative to the drawbar. Unsure where the error came from, but the threaded length of the tophat was .016 too long. This pressed firmly into the pulley and side loaded the upper deep groove ball bearings.
I turned up a plastic split bushing to hold the tophat for back work.
I indicated in the axial runout to sub .0005" and took off around .014". When reassembled, the spindle runs freely and I can tighten the tophat all the way down until the spindle hits the internal shoulder. There is still a thou or two of preload on the pulley but this is fine and helps hold it in place.
I ran the spindle up to 5000rpm for 90 minutes and here are the (relatively) steady state performance metrics:
Lower bearing temperature: 149*F
Upper bearing temperature: 153*F
Head casting (middle): 143*F
Motor (Top): 158*F
Spindle Nose: 129*F
Tool holder (End of Collet nut): 90*F
Motor running amps: 1.4A (12A = 1800W)
Heat loss into spindle assembly: 208W
Relative spindle efficiency: 89%
Noise Level: 80dBA at 3" microphone 90 degrees to machine, 73dBA at 18" microphone 90 degrees to machine
All in all, spindle runs hotter than I would like but not dangerously so. Noise level is very acceptable and no squealing, ticking, rubbing, or other bad sounds are heard.